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Clay lining example: Waranga Western Channel

On this page go to
Site preparation
Installation
Durability
Seepage reduction
Cost
Related pages

Pages in this section include:

  Earthen lining techniques
 

Compacted earthen liners

  Clay lining example: Channel 12
Clay lining example: Waranga Western Channel
  Other Australian examples
  Channel bank remodelling
  Loose earthen linings
  Bentonite treatments
  Modified soil earthen linings
  Soil sealants

Site preparation Top button

Before commencement of clay lining works, the channel was desilted and banks and batters were stripped to a minimum depth of 100mm to remove all topsoil, trees and root systems. Where the channel profile was widened to increase the capacity, channel banks were reconstructed before lining.

Installation Top button

Design features included:
  • 600mm clay lining in bed.
  • 600mm clay lining on batters.
  • 1:2.5 batter slope.
  • 300mm compacted freeboard.
  • 150mm protective cover over the bank crest to minimise shrinkage and dispersion and encourage grass cover.
Method of installation

Two techniques were adopted for the clay lining:
  1. A total length of 1,140m of the channel bed was excavated to 600mm below the design bed level and to a depth of 700mm perpendicular to the batters of the channel. Borrow material for the lining, which was hauled in from a borrow site, was placed in the bed and batters of the channel in layers of 150mm, and compacted to 98% of maximum dry density at ±2% of optimum moisture content. A 100mm compacted layer of crushed rock was then placed over the clay lining on the batters to help to maintain a constant moisture content in the clay liner, thus reducing cracking and protecting the liner from erosion. Batter slopes were no steeper than 1:2.5 so that construction machinery could achieve adequate compaction of material on the batters.
  2. A different technique was adopted for a 1,000m section due to the high shrinkage characteristics of the borrow material discovered during construction. The technique involved using material from the existing batters, mixing it with both imported clay and the degraded sandstone/siltstone from the channel bed using a stabiliser (large rotary hoe). It required double handling of material within the channel profile to enable mixing and then compaction of the bed and batters in layers of 150mm up to the 600mm depth. Only about 10% of the material required was sourced from the borrow site.
Figure 1 Aerial View of clay lining
Figure 1 Aerial View of clay lining


Specialised equipment


A stabiliser (large rotary hoe) was required to mix imported clay with the in-situ material over a length of 1,000m.

Figure 2 Stabiliser mixing insitu material with imported clay
Figure 2 Stabiliser mixing insitu material with imported clay


Installation issues

Borrow sites were identified on properties adjacent to the channel and were tested for their suitability for channel lining. Laboratory test samples were classified as CH material, which is described as ’inorganic clays of high plasticity‘ in the USCS classification system. This material has very low permeability but also has high shrink/swell potential (i.e. prone to cracking) and low scour resistance. The material was confirmed by as suitable for clay lining as it was similar to material being used in other nearby channel lining projects. Due to the high shrink/swell characteristics of the soil and the scale of the project, a protective layer of compacted crushed rock was placed over the clay liner on the batters.

During construction, soil tests identified shrinkage properties at one borrow site as unsuitable for compacted clay lining, and hence the alternative method was adopted.

At one site the excavation of the channel profile prior to clay lining exposed a large length of canal. Working ahead to this extent exposed the area to the elements and so large sections of subgrade and partly compacted clay had to be trimmed to remove wet clay from the profile following rainfall.

Durability Top button

The estimate lifespan of clay lining is 30 years, and the presence of a protective cover can extend this.

Seepage reduction Top button

A pondage test on a 480 section conducted prior to lining, identified seepage rates of 7.7L/m2/day at that site. While there has been no post-remediation monitoring of seepage rates, clay lining is expected to reduce seepage by 70-90%.

Cost Top button

The contract cost to clay-line 43,430m2 of the canal over a total length of 2,140m was $640,000 at an average of $14.74/m2. Contract rates varied for individual sections of the channel due to differences in haulage distances from the borrow sites, producing a range of lining costs from $14.25/m2 to $14.99/m2. Contract rates used assume all clay material was imported from borrow sites. Due to the nature of the lump sum contract, the actual costs for the alternative method of mixing in-situ material before compaction are not available.

Related pages Top button

Earthen lining techniques
Compacted earthen liners

Clay lining example: Channel 12
Other Australian examples
Channel bank lining
Loose earthen linings
Bentonite treatments
Modified soil earthen linings
Soil sealants
   

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Page last reviewed on 25/6/04